原料气变富对轻烃回收装置影响分析及对策

郭玉环

现代化工 ›› 2020, Vol. 40 ›› Issue (9) : 200 -203,208.

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现代化工 ›› 2020, Vol. 40 ›› Issue (9) : 200-203,208. DOI: 10.16606/j.cnki.issn0253-4320.2020.09.042
工业技术

原料气变富对轻烃回收装置影响分析及对策

    郭玉环
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Influence of feed gas enrichment on light hydrocarbons recovery unit and countermeasure

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摘要

通过对当前轻烃回收装置研究发现,原料气组分变富导致处理量下降,冷箱超过设计负荷17.69%,C3回收率下降2.64%,通过分析确定冷箱成为了装置操作的短板,提出了采用丙烷制冷系统降低脱乙烷塔顶气温度的优化对策,并计算确定单套装置的丙烷制冷系统负荷为3 000 kW。优化后冷箱负荷和膨胀机负荷降低,有利于设备的稳定运行,同时C3组分回收率达到设计值,液化气和稳定轻烃产品分别增加8.01%和4.91%,优化后的经济效益十分明显。

Abstract

It is found through researching the current light hydrocarbons recovery unit that the enrichment of feed gas components results in a decrease in the handling capacity and a decrease of 2.64% in the C3 recovery rate,and causes the load of cold box to go beyond the design load by 17.69%.Through analysis,it is confirmed that cold box becomes the bottleneck of the unit.An optimized method to drop the temperature of gas from de-ethane tower top is proposed by using propane refrigeration system,and the cold load of the propane refrigeration system for a single unit of load is determined as 3 000 kW.After optimization,the loads of both cold box and expander decrease,which is beneficial to the stable operation of the equipment,making C3 recovery rate reach the design value,and increasing the yields of liquefied gas and stable light hydrocarbons by 8.01% and 4.91%,respectively.Economic efficiency is improved obviously.

关键词

轻烃回收 / 经济效益 / 丙烷制冷 / C3回收率 / 冷箱 / 组分变富

Key words

light hydrocarbon recovery / economic benefit / propane refrigeration / C3 recovery rate / cold box / composition enrichment

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原料气变富对轻烃回收装置影响分析及对策[J]. 现代化工, 2020, 40(9): 200-203,208 DOI:10.16606/j.cnki.issn0253-4320.2020.09.042

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