中低负荷下300 MW燃煤机组SCR入口烟温提升方案设计
梅文 , 王峰 , 武洁 , 周会成 , 唐忠锋
现代化工 ›› 2025, Vol. 45 ›› Issue (12) : 219 -223.
中低负荷下300 MW燃煤机组SCR入口烟温提升方案设计
Design of SCR inlet flue temperature enhancement program for 300 MW coal-fired units under low and medium loads
The selective catalytic reduction denitrification reaction (SCR) system cannot operate due to a low inlet flue gas temperature when the coal-fired units in thermal power plant operate at low and medium loads.To address this issue,a 300 MW coal-fired unit of a power plant is taken as the research object,a joint design scheme combining feedwater bypass with flue gas bypass is employed to analyze the change of the inlet flue gas temperature of the SCR.Aspen Plus software is utilized to establish a wide-load denitrification model,and the flow rate is adjusted to raise the SCR inlet flue gas temperature according to the temperature rise requirement.Study results show that as the maximum continuous evaporation of the boiler stays at the load range of 20%-86%,the joint design scheme has a 0.1%-1.19% impact on the thermal efficiency of the unit,the flow regulation amount is 3%-8% lower than the total regulation amount by separated input,the temperature of the inlet flue gas is increased by up to 50℃,the denitrification efficiency is increased by up to 31.5%,and the emission concentration of NOx is lower than 36.8 mg/m3.This scheme can help SCR realize the stable operation when the maximum continuous evaporation amount of the boiler exceeds 20% load,and meet the emission requirements.This study provides solutions for the problem that NOx concentration surpasses the emission standard due to low SCR inlet flue temperature caused by variable load operation of coal-fired units under deeply peak shaving.
深度调峰 / 燃煤机组 / 火电厂 / 温度 / SCR / NOx
deeply peak shaving / coal fired unit / thermal power plant / temperature / SCR / NOx
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内蒙古电力(集团)有限责任公司内蒙古电力科学研究院分公司项目(2024-ZC-2-02)
中央引导地方科技发展奖励资金项目(2023ZY0006)
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