低碳烷烃脱氢丙烯精馏系统优化设计

高海见

现代化工 ›› 2023, Vol. 43 ›› Issue (3) : 217 -220.

PDF (1413KB)
现代化工 ›› 2023, Vol. 43 ›› Issue (3) : 217-220. DOI: 10.16606/j.cnki.issn0253-4320.2023.03.040
工业技术

低碳烷烃脱氢丙烯精馏系统优化设计

作者信息 +

Optimization of propylene distillation system in light alkane dehydrogenation plant

Author information +
文章历史 +
PDF (1446K)

摘要

通过对某60万t/a烷烃脱氢装置丙烯精馏系统进行分析发现,设计中采用的塔板效率过低是造成塔的操作能耗偏高的主要原因。选取塔板效率95%,通过PROII软件对此精馏塔进行模拟,在实际塔板数不变的情况下,回流比可降低至18.76,塔顶和塔釜热负荷可分别降低至-428.0 MkJ/h、437.2 MkJ/h。在此基础上对温水系统进行改进,可取得节省2 772.4万元投资和节省操作费用768万元/a的效果,同时简化了操作流程。

Abstract

Based on the analysis to the propylene distillation system of a 600 000 t/a PDH plant,it is found that the low efficiency of the trays employed in the design results in excessive energy-consumption in the operation of the distillation tower.By selecting 95% as tray efficiency,the propylene distillation tower is simulated through PROII software.Result shows that the reflux ratio can drop to 18.76,the duty of tower condenser and reboiler can decrease to -428.0 MkJ·h-1 and 437.2 MkJ·h-1 respectively while the actual number of trays remains unchanged.On this basis,the warm-water system is modified,which can save RMB 27 724 000 of cost and RMB 7.68 million per year of operating cost.

关键词

烷烃脱氢 / 流程优化 / 丙烯精馏塔

Key words

alkane dehydrogenation / process optimization / propylene distillation tower

引用本文

引用格式 ▾
高海见. 低碳烷烃脱氢丙烯精馏系统优化设计[J]. 现代化工, 2023, 43(3): 217-220 DOI:10.16606/j.cnki.issn0253-4320.2023.03.040

登录浏览全文

4963

注册一个新账户 忘记密码

参考文献

AI Summary AI Mindmap
PDF (1413KB)

433

访问

0

被引

导航
相关文章

AI思维导图

/