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摘要
结合鲁西化工集团股份有限公司现有粉煤加压气化装置的运行情况,对停运固定床造气炉后的原料气来源进行探究,提出了将低温甲醇洗工序的净化气、PSA工序的解析气、CO膜分离工序的渗透气送至氮氢气压缩机的改造方案。通过对原料气路线的改造,既减少设备闲置、提高设备利用率,又提高生产效率。
Abstract
Combined with the operation situation of the existing pulverized coal pressurized gasification unit of Luxi Chemical Group Co.,Ltd.,the disadvantages of batch fixed-bed gasification technology are analyzed,and the source of raw material gas after stopping the fixed-bed gasifier is explored.A renovation scheme is proposed for raw material gas route by sending the purified gas after the low-temperature methanol washing section,the desorption gas after PSA section,and the permeate gas after CO membrane separation section to the nitrogen-hydrogen compressor.After renovating the raw material route,the idle equipment is reduced,both the equipment utilization and the production efficiency are improved.
关键词
甲醇
/
设备利用
/
技术改造
/
原料气
/
联产
/
合成氨
Key words
methanol
/
equipment utilization
/
innovation
/
raw material gas
/
co-production
/
synthetic ammonia
合成氨联产甲醇装置原料气路线的改造及实效[J].
现代化工, 2020, 40(5): 214-218 DOI:10.16606/j.cnki.issn0253-4320.2020.05.047